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Numerical and experimental investigation on the effects of aft mixing chamber diaphragm in hybrid rocket motor

Numerical and experimental investigation on the effects of aft mixing chamber diaphragm in hybrid rocket motor

作     者:TIAN Hui LI XinTian YU NanJia CAI GuoBiao 

作者机构:School of AstronauticsBeihang University 

出 版 物:《Science China(Technological Sciences)》 (中国科学(技术科学英文版))

年 卷 期:2013年第56卷第11期

页      面:2721-2731页

核心收录:

学科分类:0810[工学-信息与通信工程] 080703[工学-动力机械及工程] 08[工学] 082502[工学-航空宇航推进理论与工程] 0807[工学-动力工程及工程热物理] 0805[工学-材料科学与工程(可授工学、理学学位)] 0825[工学-航空宇航科学与技术] 0702[理学-物理学] 0812[工学-计算机科学与技术(可授工学、理学学位)] 

基  金:National Natural Science Foundation of China  NSFC 

主  题:hybrid rocket motor diaphragm numerical simulation experimental investigation 

摘      要:This paper focuses on the investigation of an aft mixing chamber diaphragm in a hybrid rocket motor. Both numerical and ex- perimental researches are carried out to study its effects on the motor performances. The hybrid rocket motor with star fuel grain is utilized. The 90% hydrogen peroxide (HP) oxidizer and hydroxyl terminated polybutadiene (HTPB) based fuel are adopted as propellants. The diaphragm configuration settled in the aft mixing chamber includes four circular-holes with a uni- form circumferential distribution. For both motors with and without the diaphragm, three-dimensional numerical simulations with gaseous combustions considered are carried out to study the flow field characteristics and motor performances. The com- parison results show that the diaphragm can improve the mixing of the oxidizer and fuel. It has evident effect on increasing the motor efflciencies. Two firing experiments are conducted with full scale motors to investigate the effects of the diaphragm. The diaphragm used in the test is composed of a central steel framework and a closed thermal insulation layer. With the dia- phragm employed, the combustion efficiency increases from 93.9% to 97.34% and the specific impulse efficiency increases from 80.77% to 87.28%, which verifies the positive effect of the diaphragm. Both numerical and experimental studies indicate that the scheme of the aft mixing chamber diaphragm proposed in the paper can improve the efficiencies of the hybrid rocket motor obviously.

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